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Post by angelislington on May 15, 2009 8:51:22 GMT
A friend of MRFS42's & mine is a diseasel engineer, and he recently posted the following on another forum we're on: Pics available here. indeed!
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Post by geebeezed on May 15, 2009 10:33:10 GMT
Kinda reminds me of such an incident on one of the old Thumper units we used to have running across the Marsh, I think it was 207203... One winter's day the Driver reported hearing a load of noise & lots of smoke from the Engine room on departure from Appledore and the unit losing one cylinder, the engine kept running so he kept on driving up to Ashford figuring it'd be easier for someone to investigate at a proper depot... And so we opened the engine room door on arrival, to find the whole thing soaked in oil, one of the crankshaft inspection hatches missing and a Piston & conrod lying on the floor! Another time on a similar unit, the Driver reported a loss of power but again, kept going... This tme when the fitters arrived they found the entire turbocharger had fallen off its mounts & exited through one of the side windows! I'm not sure they ever found it!
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Post by Deleted on May 17, 2009 11:07:17 GMT
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Post by Deleted on May 17, 2009 18:16:05 GMT
Kinda reminds me of such an incident on one of the old Thumper units we used to have running across the Marsh, I think it was 207203... One winter's day the Driver reported hearing a load of noise & lots of smoke from the Engine room on departure from Appledore and the unit losing one cylinder, the engine kept running so he kept on driving up to Ashford figuring it'd be easier for someone to investigate at a proper depot... And so we opened the engine room door on arrival, to find the whole thing soaked in oil, one of the crankshaft inspection hatches missing and a Piston & conrod lying on the floor! Oh yes... wasn't the driver hoping he got a clear signal into platform 1 too?
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Post by Deleted on May 27, 2009 17:46:16 GMT
A Westbury based Driver was given a class 37 for the Woking stone job one day in the late 1990s despite the powers that be knowing about his complete detestation of the type. Control and the supervisors were ready for him and had asked the Westbury acting instructor to prepare it for him so that he couldn't find anything 'wrong' with it.
He set off, moaning, and that was that so they thought. A couple of hours later control got a phone call from him. '37709 on the Woking Stone is a failure and I need a replacement locomotive'. Control replied 'Oh yeah! What convoluted fault do you think you have on this one today then?'. Driver replied 'I think that the loco has suffered a big-end failure'. Control asked 'Ok smart@#$£. What makes you think that then?'. Driver:- 'Because I'm holding part of one of the bearings in my hand!'.....
I had a look over the loco after it was towed to Eastleigh and 'A' bank of the engine was a mess! The engine has two, presumably cast, inspection covers at the bottom end of the crankcase. One of these had been blown outwards and bent into a dome shape shearing the bolts that held it in place. Shrapnel covered the internal walkway.
The best bit for us Eastleigh men was that the Driver who was sent up to Woking to tow it back with a class 73 was the biggest class 37 crank on the planet! he was almost in tears when he got back!
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